More about improving your A10.

Braking

Riding two up 95% of the time means that braking was a major consideration and because of this big changes have been made front and rear. At the front I have fitted a twin leading shoe brake available in 1969 and early 1970 before the conical hubs were introduced. This fits straight into a full width hub as fitted to my 1961 bike. The only mod needed is to extend the brake plate location boss on the right hand fork leg by about 1/8" to locate the plate more securely. The cable fitted has a brake light switch incorporated in it so braking indication is given when both brakes are used. At the rear I despaired of finding a decent cable that wouldn't snap under heavy braking. Having snapped four of these I decided a change to rod operation was the only solution and set about designing something more solid. The result was a 5/16" stainless steel rod bent in two places like a stretched Z to allow it to go behind the suspension unit. A new torsion arm was made with holes spaced an extra inch. This swings the brake plate round by about 15 degrees and moves the brake arm higher. This actually brings it to the same position as the earlier brake in which the cable lies above the wheel spindle. An early A65 brake actuating arm was bought and fitted on the crossover shaft. The ends of the brake rod were threaded and stainless clevis's bought from an army surplus store were screwed on. These are screwed up or down the rod to give brake adjustment. The slight flexing of the rod does tend to give the brake some "feel" and it is now possible to lock the back wheel with no danger of snapping anything.

Electrics

A K TEC regulator provides 12 Volts, allowing the use of a quartz halogen headlamp and pilot bulb. The 20 Watt pilot bulb means I can run with a visible light during the day. The regulator copes with this easily. 40 degrees celsius heat made it difficult to ride during the day to the Italian International Rally so the last 250 miles were done at night lighting the way sufficiently to cruise at 65 - 70 mph with no problems. Eat your heart out Joe Lucas, Prince of Darkness. When I rewired the bike I incorporated a hidden isolator switch, 30 amp fuse and a 1/4" jack socket to give a power feed for auxiliary equipment e.g. fluorescent light for the tent and electric pump for the airbed. We like a little comfort when camping.

Suspension

To allow for continuous 2 up riding with all the equipment we carry it was also necessary to fit heavy duty springs in the forks and stronger shocks at the rear. I don't know how strong the rear springs are but after stripping them for repainting I had such a job compressing them during rebuilding I don't want to ever strip them again.

Cables

All control cables are doubled up, this allows easy replacement when one snaps, so next time you have the tank off it might be a good idea to tape a spare clutch and throttle cable alongside those in use. I snapped my throttle cable in the Lake District a few years ago on a run out at a Manchester Branch Camp and amazed some people when I was up and running again within 15 minutes.

Comfort

Latest addition has been a different seat. Long distance travel on the standard item has always taught us the real meaning of BSA B...DY SORE A...HOLE. So when I looked at the new seat I bought for our Rocket Three I realised it wouldn't take too much work to make it fit the A10. One trip to Italy and 1900 miles later in just over a week confirmed my initial belief, the seat is staying.

Gearing

It has always been my belief that the A10 is undergeared and experimenting with different cogs on crank and gearbox I settled on all standard cogs but for the engine sprocket, which has been changed from the standard 21 tooth to a 22 tooth. This means I am now changing up into top at about 35 mph and 40 - 45 mph under acceleration. The bike has coped well with the mileage and strain, the only parts suffering being the rear chain and sprocket. - 10,000 miles being all that could be expected from a Renolds chain. Changing to a DID50 chain has increased life by 20%. We've also worn out 5 sets of pillion footrest rubbers in the last 70,000 miles. When did you last have to change yours?

Carburettor

Lumpy running and erratic tickover after about 10,000 miles was cured by sending the carburettor to Martyn Bratby for resleeving. It is still performing perfectly. I thoroughly recommend his work. Spares have been supplied by C + D Autos (10% discount to BSAOC members), Lightning Spares, my local dealer and Anglo Moto at autojumbles and over the phone sometimes. Thanks Pat Arnold of Anglo Moto for coming to the rescue more than once. Mind you it has cost me some beers. One major problem we had was terrible vibration after 50,000 miles which was eventually traced to those worn crankshaft splines I mentioned earlier. The engine was stripped and the crank sent to SRM for welding and remachining. When it was returned the sprocket sleeve fitted like a glove. Due to the oil feed conversion the big ends were still within tolerances, so as a matter of course new shells were fitted, along with a new drive side bearing. SRM supplied both and incidentally the bearing cost the same as it did five years earlier. The A10 has been in semi retirement for the past few years since we got the Rocket Three on the road but gets aired occasionally, included being borrowed by various visitors from all over the world. I have already started working on modifying the Rocket Three and am currently working on an article on this machine at the moment. We hope you enjoyed reading the article and find at least one of the modifications useful.
BSAing you
Brian and Chris Pollitt
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